22 Rigs. 4 AM. One Summary.
Barrel synthesizes overnight drilling reports, NPT events, frac crew status, and cost tracking into a single briefing — before your morning call.
Overnight summary — 22 rigs, 4 frac crews:
| Drilling on plan | 19 | |
| NPT events | 2 | Rig 8 (motor failure), Rig 15 (weather) |
| Frac on plan | 3 | |
| Frac NPT | 1 | Crew 4 (pump down issue, 6hr est) |
Total NPT cost overnight: ~$420K. Rig 8 motor replacement ETA 14:00 today. Weather hold on Rig 15 should clear by 08:00 per NWS forecast. Recommend moving Frac Crew 4 to standby well if pump issue exceeds 12hr.
Before and After Barrel
5 AM: overnight IADC reports from every rig. Each rig generates gigabytes of daily data. 6 AM drilling call — rig by rig: depth, footage, ROP, well control, days vs AFE. Then completions, frac crews, vendor calls.
Barrel's overnight synthesis: 22 rigs summarized, 2 NPT events flagged with cost estimates, frac crew status, AFE variances highlighted. Your drilling call starts with decisions, not data collection.
Built for the Morning Call
Multi-rig overnight synthesis — every rig summarized with exceptions flagged
NPT tracking and cost — downtime events with estimated cost impact
AFE variance monitoring — per-well cost vs authorization, trending analysis
Frac crew coordination — stage counts, pump-down status, schedule optimization
Weather and logistics — road closures, rig moves, water hauling
AFE Variance
AFE variance — active wells:
| Well 14-H | $8.2M vs $7.3M AFE | +12% — casing issue at 8,400ft |
| Well 22-H | $6.1M vs $6.8M AFE | -10% — ahead of plan |
| Well 9-H | $4.9M vs $5.0M AFE | -2% — on track |
Well 14-H variance driven by 3 extra casing runs at 8,400ft — lost circulation zone. Drilling engineer recommends LCM pill before next section. If successful, final cost estimate drops to $7.8M (+7% vs AFE).
Frac Crew Status
Completions status — 4 frac crews:
| Crew 1 | 28 stages today | Well 18-H — on schedule |
| Crew 2 | 32 stages today | Well 6-H — 2 stages ahead |
| Crew 3 | Mobilizing | Pad 7 — frac starts Mar 8 |
| Crew 4 | NPT — pump down | 6hr est, standby well ready |
Crew 4 pump-down issue: iron plug stuck at 7,200ft. Wireline crew en route — ETA 2 hours. If not resolved by 14:00, recommend moving to standby Well 11-H. No impact on monthly stage count target.
NPT Alert
Rig 8 motor failure — replacement ETA 14:00 today
5:30 AM
AFE Variance
Well 14-H running 12% over AFE — casing issue at 8,400ft
6:15 AM
Weather Hold
Rig 15 shut down — NWS forecast clears at 08:00
4:45 AM
Connects to Your Stack
Measured Impact
22 rigs
1 summary — operational synthesis
Minutes
NPT detected — not hours
AFE flagged
Variance caught before it's a surprise
Start Your Operations Briefing
Tell us about your workflow. We configure Barrel for your role, data sources, and reporting cadence.
No credit card. No setup fee. We configure Barrel for your workflow.